PHILIPE
Veteran Member
Surprising that this has not made the forum but yesterday, GWR 1F09 0930 Cardiff to Portsmouth Hbr, became a complete failure inside the Severn Tunnel and worked by a pair of Turbos 165131 and 166209 (5 carriages in all). I cannot go back to Quote anything at this stage due to any items disappearing from the system with the train.
The train eventually came out of the Tunnel 146 minutes late but information is rather patchy.
Trains were allowed through on the Down Line after a time under Reversible working and each time the driver wanted to go onto the ground to deal with the issue the signaller had to be asked to put a block on. This would have been more difficult due to no through corridor access between the two units. Eventually an additional traincrew were dispatched to the scene and the train was finally split and came out in separate portions. If I receive information re the actual fault I will post it.
The train eventually came out of the Tunnel 146 minutes late but information is rather patchy.
Trains were allowed through on the Down Line after a time under Reversible working and each time the driver wanted to go onto the ground to deal with the issue the signaller had to be asked to put a block on. This would have been more difficult due to no through corridor access between the two units. Eventually an additional traincrew were dispatched to the scene and the train was finally split and came out in separate portions. If I receive information re the actual fault I will post it.