23/2/17- The Storm Doris Bash. Day 2: Oh Jesus
Doing things a bit backwards here
Well this was a day that had already been changed a number of times due to the weather, and i’ll be honest I wasn’t massively looking forward to dealing with the suddenly expected carnage that was initially not meant to affect as far south as Birmingham! Nonetheless, I checked out of my hotel at 0550 and headed for Chester station, picking up a Costa and bacon sandwich before awaiting the swift arrival of winner
175007 on the 0618 to Cardiff via Wrexham. There weren’t many on board on departure, and it was a boring run in the dark down to Shrewsbury, before things lightened up and it was a genuinely pleasant dash through the Marches until Ludlow and Leominster where the admittedly quiet students of a school in Hereford joined us, and that was also where I left the train at 0810, making it shack number 1. I headed out through the gates and bought a single to Ledbury as well as a West Midlands Ranger for the day, before taking cover as the winds started to pick up a fair bit. Eventually, dud
170517 leading winner
153365 trundled in, and I sat in the 153 for a pleasant run out as far as Ledbury where the disruption was already starting as the inbound service to Hereford was 25L.
I jumped off there and grabbed a few photos, which was enough for me to count it as a score as I had a wander around, chatted with the guard and jumped back on just before we resumed, where I bailed at Great Malvern, shack 3. This was a pleasant enough station and I had 10 minutes or so before winner
180106, my first GW 180, made its shunt moves and proceeded to form the Paddington service. Annoyingly however, none of the sockets were working for the journey to shack 4, Worcester Shrub Hill, where it was a quick swap onto winner
150124 back to Worcester Foregate Street. Everything seemed to be okay again as I picked up dud
170509 which was only 2 minutes late on the New Street service, and I intended to jump off at University and do the shacks down to Redditch. However, as we left Droitwich Spa, I noticed that the Cross City services seemed to have stopped running with a few others running quite late. Drat. After Bromsgrove, we were utterly rammed as we did a very slow stop journey as far as Kings Norton where I noticed that there were a lot of 323s queued up on the other line. An announcement was then made that the line was blocked at Five Ways, and so we’d be diverted via Camp Hill and would no longer call at University.
Oh well, I guess I could just avoid wires for the day then. New track scored via Camp Hill and I arrived into New Street 14L to the sight of further carnage with barely anything running at all. That was my cue to make a hasty dash to Moor Street and dive onto winner
172218 leading dud
172220 to Jewellery Quarter. I made the VERY sensible decision to not venture too far and to attempt some red pen moves, which ended badly with dud
172345 up to The Hawthorns and duds
172214/172221 back to Jewellery Quarter. The service on the Snow Hill Lines was then duly suspended without anybody telling us, with everything showing as ‘delayed’ until I gave up after 35 minutes of waiting and joined dud Tram
36 to Grand Central. I wasn’t even sure if there was ticket acceptance, but common sense dictated that if absolutely everything had been cancelled then I should have been able to use Midland Metro. As it turns out, everything was fine and I was soon looking around at New Street to see what was actually running.
The 1239 to Wolverhampton seemed to exist, so I jumped on dud
350237 to my last New Street-Wolves shack, which was Coseley. We were 11L and the next service was oddly on time, so I hung around here in the waiting room until winner
350266 turned up to Wolverhampton, where there seemed to be some optimism as there was a Liverpool service operating and there were Crewe to Birmingham trains running again. I jumped on a delayed winner
350245 to shack 6, Penkridge, which was my last shack between Crewe and Brum, and was meant to be joining a service straight back south after about 10 minutes. We were delayed by 48 minutes into Penkridge (as we seemed to run into the Four Ashes Loop and straight back out) and I jumped off onto the very windy station only to find that my intended service wasn’t exactly intending on turning up any time soon. Indeed, it limped into Stafford at 1430 and after 55 minutes of noting that the service was belly up again, I ordered a taxi (£15 that I didn’t wanna spend!) to Stafford.
The taxi turned up fairly sharp and the friendly chap took me along through the country roads so as to avoid congestion en route (and promised that this would do nothing to the price), even letting me get cash out on arrival as I only had my card. Arrival was at around 1525 and I noted that there was an apparent Lime Street train due at 1601, so I kicked myself for not waiting around longer. However, a service on Platform 5 caught my interest. Dud
390136 was working the delayed 1020 Euston-Piccadilly and had made an additional call so I made myself at home, put my phone on charge and sat around awaiting announcements. We stayed like this for over two hours, with announcements coming over that there was no way north or south for the time being, which was bizarre as the Liverpool Desiro eventually came past at 1705 and departed straight away (I didn’t care much, it was dud 350101 and i’d have been stranded as Crewe had I joined it) but we were at least given refreshments. Departure miraculously came around at 1727 (I was resigning myself to staying with a friend in Whitchurch for the night) and we ambled our way around to Manchester, a comical 377 minutes behind the original schedule at 1845. However, I was just thankful that the train had stopped at Stafford otherwise i’d have been stuck with a STP XC Voyager service which eventually arrived Manchester 1949 and would have saw me into Newcastle at 2351!
Dud
185146 was working the 1857 to Middlesbrough and I jumped on as I saw no point in awaiting my booked service at 1942, which got me into York at 2016 where I went off to a local Spar for three pasties (knocked down to 33p each!) and awaited the delayed 1945 to Newcastle which was formed of a dud
220013, arriving Newcastle 2148, 66L.
An awful day but I couldn’t have done anything to help myself, if anything I dodged multiple bullets! And it was new track from Shrewsbury to Hereford and onwards to Malvern Link, so I still achieved something along with a smattering of shacks and winners (including the celebrity 153365
)
The actually successful day will be along shortly!
Total Mileage: 380mi 78ch
Total winners: 7+6 shacks