I managed to time it so that I got the absolute worst of the disruption on Saturday, and I can tell you it was
not good.
The long and short of it was that I planned to take the 2233 Dunblane service to Linlithgow, but didn't arrive back in Linlithgow until after 2430. To say that this situation was handled poorly by ScotRail would be the understatement of the year. Yes, it was Festival time, and yes there was a game on at Murrayfield. Yes, it's difficult to get all the staff needed to put on services during a bank holiday weekend. And it's absolute worst case stuff when a new train breaks down at a critical time. But with that in mind, here's what went wrong:
- Communication was appalling. Most of the information we received was given by extremely flustered and thinly stretched BTP officers. ScotRail staff were nowhere to be seen, information boards were useless, station announcements basically non-existent.
- Most irksome, is that services which were clearly never going to run were still advertised as leaving on time, from a certain platform, until about 15 mins after their scheduled departure time, creating massive choke points and unsafe levels of overcrowding on platforms and ticket gate areas as people fled from one platform to another, repeatedly, for another service that was not going to run (and whose rolling stock was never even going to arrive). In our case, the 2245 and 2316 simply never ran, not a single explanation given as to why not... but both were assigned platform numbers which had hordes of people running in different directions as a result. Why do this?!?
- This statement about ScotRail running every train they had available... I just don't buy it. Given that ScotRail can run 4x 7/8car, and 4x 4car 385 services from Waverley to Queen Street and Dunblane at peak, why did so many services simply not turn up, and why was the 2330 Waverley to Queen Street running as a 6 car 170, and the 2334 to Dunblane a 5 car 170/158 hybrid? The massively reduced capacity meant that the vast majority of passengers couldn't physically get on the 2330. This, despite the fact that many passengers going straight to Glasgow were using the AtoB services instead. I'll be willing to back down on this if someone can provide a credible justification for why this happened.
- ScotRail's usually helpful twitter account was simply suggesting that we make "alternative transport arrangements" to get home. I'm sorry, what?! How?!
- It really didn't help that many people were drunk - and that a small portion of the general public didn't make matters any better here. The passengers in some cases could have behaved far, far better. However on the whole people were well behaved, and given the choke points that we were funnelled into around the ticket gate area, to be honest, things could quite have easily gone far worse. I'm actually amazed, in that instance, how calmly everyone behaved.
The simple fact is, is that time and again when it comes to the days that ScotRail really needs to step up and perform, it is found wanting. Someone on the 385 thread said that when ScotRail does things well, it does them very well, but when things go wrong, they go very wrong. I agree with this sentiment. I don't mind crowded trains, standing room only etc; as someone pointed out that in London this is par for the course during commuting hours. However when it's late at night and everyone is pretty drunk, that makes for a very different experience; a far less controllable and predictable one. Even worse when they were so over-packed that hundreds of people can't even get on them. I feel genuinely sorry as well, for tourists caught up in this. I'd say it must have been pretty unsettling, and embarrassing that we simply can't get the big moments like this right. Did we ever find out what actually happened to the broken down 385?