Spamcan81
Member
Hi,
Newby here.
The strip down of 34081 is almost complete and we'll soon begin the long and painstaking task of reassembly. In the meantime Chatham Steam is getting on with the boiler overhaul and currently making good progress.
An extract from Kingsley's (one of the overhaul team) blog.
"August 31st.
Another great turnout today.
Roger. Got stuck into the bogie chassis cleaning.
Doc. Started the stripping of the primer on the Delta which the faulty Phosphoric acid had allowed the rust to leach through.
Alan.P. Was working with Roger on the bogie. Alan is also starting a log of member's hours worked on the loco.
Mick. Was cleaning and prepping the whistle operating rod assembly and was last seen attempting to prime an 18ft length of 1/4" dia rod which was behaving like a snake.
Ambie. Still on the chassis clean and now with the new cleaning agent that Al got, even better.
Alan.C. Worked on the drag box with the needle gun.
Barry. Valiantly attempting to repair the fine mesh gauze in one of the sump breathers.
Richard. P. Bought up the laptop which has kindly donated for our logging records.
Alan got stuck in to some paint jobs and has taken the shed plate away to highlight the white on the plate. He also gave Ambie assistance on the 'higher' sections of the chassis clean.
DOC. Although involved with 656 was also involved under the front end on the linkage for the drain cocks.
Graham. Working under the front end removing the three centre cylinder drain cocks and the linkage.
Jim. Also working with Graham and then subsequently temporarily reassembling the cocks and linkage for photos.
Mike. Tackled the rear diaphragm plate. We 'suggested' he did this outside as the the needle gun produced well serious noise!
Myself. Cleared some items into the green, top coated the axle and horn block lubrication assemblies, found the whistle shaft assembly, tagged and photographed the centre drain cocks and linkage in situ and reassembled after removal/
13 people today and all busy. It's really wonderful to see such turnouts and the lovely atmosphere being generated. Long (but not too long) may it continue.
We now know that when she goes back into traffic, we will have a very strong support team for Al on the service and maintenance front as every one will have have proper hands on experience."
Newby here.
The strip down of 34081 is almost complete and we'll soon begin the long and painstaking task of reassembly. In the meantime Chatham Steam is getting on with the boiler overhaul and currently making good progress.
An extract from Kingsley's (one of the overhaul team) blog.
"August 31st.
Another great turnout today.
Roger. Got stuck into the bogie chassis cleaning.
Doc. Started the stripping of the primer on the Delta which the faulty Phosphoric acid had allowed the rust to leach through.
Alan.P. Was working with Roger on the bogie. Alan is also starting a log of member's hours worked on the loco.
Mick. Was cleaning and prepping the whistle operating rod assembly and was last seen attempting to prime an 18ft length of 1/4" dia rod which was behaving like a snake.
Ambie. Still on the chassis clean and now with the new cleaning agent that Al got, even better.
Alan.C. Worked on the drag box with the needle gun.
Barry. Valiantly attempting to repair the fine mesh gauze in one of the sump breathers.
Richard. P. Bought up the laptop which has kindly donated for our logging records.
Alan got stuck in to some paint jobs and has taken the shed plate away to highlight the white on the plate. He also gave Ambie assistance on the 'higher' sections of the chassis clean.
DOC. Although involved with 656 was also involved under the front end on the linkage for the drain cocks.
Graham. Working under the front end removing the three centre cylinder drain cocks and the linkage.
Jim. Also working with Graham and then subsequently temporarily reassembling the cocks and linkage for photos.
Mike. Tackled the rear diaphragm plate. We 'suggested' he did this outside as the the needle gun produced well serious noise!
Myself. Cleared some items into the green, top coated the axle and horn block lubrication assemblies, found the whistle shaft assembly, tagged and photographed the centre drain cocks and linkage in situ and reassembled after removal/
13 people today and all busy. It's really wonderful to see such turnouts and the lovely atmosphere being generated. Long (but not too long) may it continue.
We now know that when she goes back into traffic, we will have a very strong support team for Al on the service and maintenance front as every one will have have proper hands on experience."