theironroad
Established Member
- Joined
- 21 Nov 2014
- Messages
- 3,717
Tbh, I can't remember if SR have ticked all the boxes for the DCC grant, but either way, I can#t see the council demanding any money back.Yes lets forget about the £5M+ of tax payers money that was spent on this project.
The "lets forget about it" attitude - and I have to say that was my interpretation of reading Swanage Railway Magazine - concerns me deeply. It shows an unwillingness to learn from this project of which there are so many learnings not least a failure to listen to all those who had justifiable doubts but were labelled as doom mongers by the SRT and SRC.
They have lost a great deal of goodwill in the local community (as evidenced by the comments on the Swanage News Facebook pages) and will have lost a great deal of credibility with Dorset Council and Swanage Town Council.
Coincidentally, and I accept it is pure coincidence, but the majority conservative groups on both councils who were supportive of SRC are no longer in power in the case of Dorset Council and there is a hung council at Swanage Town Council. Mike Whitwam a long term SRT Trustee and formerly a long term Director of SRC has lost his seat on Swanage Town Council.
Whilst the T3 has been a fantastic success - of which SRT SRCs part has been to raise the funds for it to be restored professionally off railway - there are a number of long term projects which are stalled and have been for a long time due to lack of funds: the water tower project, the turntable project and the two unrestored moguls.
They talk about not wishing to compete with the local bus service and cite the £2 fares but that was not the market they were seeking to attract. The market they were seeking to attract was the tourist coming from further afield, persuading them to leave the car at home and in conjunction with SWR come by train all the way. Does SRC really believe that the bus fare reducing from £9 return (IIRC) to £4 return dealt a fatal blow? That the Wareham passenger numbers pro rata are not very different from 2017 when there was no cheap bus fare rather undermines their argument.
They have blamed covid, the cost of living crisis, the £2 bus fare, the refurbishers of the DMU Units for delays and cost overruns, the bad luck that every axle on the dmus failed the crack inspection test, the cost of compliance for mainline running. Is it bad luck or something else?
If things are as a dire as the article suggested then, then the core focus and restructure is the only way forward.