• Our new ticketing site is now live! Using either this or the original site (both powered by TrainSplit) helps support the running of the forum with every ticket purchase! Find out more and ask any questions/give us feedback in this thread!

WCML Signal 113 (near Primrose Hill tunnel) fault

Sponsor Post - registered members do not see these adverts; click here to register, or click here to log in
R

RailUK Forums

Nippy

Member
Joined
13 Aug 2013
Messages
701
I don’t actually know I’m afraid. We (signallers) were just told it could be booked back into use.
 

alxndr

Established Member
Joined
3 Apr 2015
Messages
1,603
But when they were first installed they weren't a problem so whats changed since their installation?
I don’t know in this specific case, but components can degrade overtime and become less effective at filtering out interference or cables can be damaged. The level of interference can also increase beyond what can be filtered out, this has happened in a few different places where there has been issues with the overhead line switching equipment.
 

Annetts key

Established Member
Joined
13 Feb 2021
Messages
2,977
Location
West is best
But when they were first installed they weren't a problem so whats changed since their installation?
The interference may have come from a faulty item of signalling equipment. Or other nearby equipment.

Or part of the datalink (cable or equipment module connected to it) have have degraded resulting in a worse signal to noise ratio. Like listening to an AM radio, then a car passes with an unsuppressed ignition system and the audio signal becomes hard to hear due to the interference.

The trouble is, with up to 63 Trackside Functional Modules (TFM) per data link, tracking down the source of the trouble is time consuming.
 

Tilting007

Member
Joined
21 Oct 2024
Messages
143
Location
Rugby
The reason for the failure here is still under investigation.
The only change is approach control on Fast Lines has been removed.
 

MarkyT

Established Member
Joined
20 May 2012
Messages
7,000
Location
Torbay
The interference may have come from a faulty item of signalling equipment. Or other nearby equipment.

Or part of the datalink (cable or equipment module connected to it) have have degraded resulting in a worse signal to noise ratio. Like listening to an AM radio, then a car passes with an unsuppressed ignition system and the audio signal becomes hard to hear due to the interference.

The trouble is, with up to 63 Trackside Functional Modules (TFM) per data link, tracking down the source of the trouble is time consuming.
In addition to interference from railway sources such as traction, it's plausible third party activity near the railway can cause problems, say a really noisy electrical process under the line in a commercially leased arch, or a powerful new radio transmitter nearby. Unfortunately BR chose a copper datalink standard while Belgium specified fibre optics for the same job when they also adopted SSI technology through Alst(h)om (a little later than BR I think to be fair). While Belgium used the same central interlocking hardware, they had different custom TFMs, datalink modules and customised main programme and data config language that better matched their national standards. I think the field address space was larger, i.e. more modules per system, and the fibre datalink protocol was much faster and suitable for axle counter evaluation over the same link. Alstom developed a special TFM that, in addition to standard inputs and outputs, could directly connect the inductive sensors.
 

alf

On Moderation
Joined
1 Mar 2021
Messages
392
Location
Bournemouth
The reason for the failure here is still under investigation.
The only change is approach control on Fast Lines has been removed.
This fault caused considerable disruption over many weeks.

If the approach control, which caused many down fast drivers to slow to 10mph from 55 mph, can be removed now with the ‘failure’ still under investigation why was approach control ordered in the first place.

For the signallers’ & the public’s benefit I hope this fault can be eliminated & publicly explained so lessons can be learnt.
 

najaB

Veteran Member
Joined
28 Aug 2011
Messages
32,331
Location
Scotland
If the approach control, which caused many down fast drivers to slow to 10mph from 55 mph, can be removed now with the ‘failure’ still under investigation why was approach control ordered in the first place.
I'm not in he industry so this is purely speculation, but my guess would be that they initially defaulted to the safest mode of operation per the rule book (approach control) until they were able to make the safety case for resuming normal operating procedures.

In other words, assume that it will kill you until you can prove that it won't. Don't forget that the rules are literally written in blood.
 

Tilting007

Member
Joined
21 Oct 2024
Messages
143
Location
Rugby
I'm not in he industry so this is purely speculation, but my guess would be that they initially defaulted to the safest mode of operation per the rule book (approach control) until they were able to make the safety case for resuming normal operating procedures.

In other words, assume that it will kill you until you can prove that it won't. Don't forget that the rules are literally written in blood.
This fault caused considerable disruption over many weeks.

If the approach control, which caused many down fast drivers to slow to 10mph from 55 mph, can be removed now with the ‘failure’ still under investigation why was approach control ordered in the first place.

For the signallers’ & the public’s benefit I hope this fault can be eliminated & publicly explained so lessons can be learnt.
To prevent a SPAD at line speed. It will not have been applied for the fun of it - and the delay will have caused significant financial penalty to NR.

Still in under investigation means the exact cause may not be known but there is enough data and enough has been done to stabilise the link enough to remove the approach control.
 

Annetts key

Established Member
Joined
13 Feb 2021
Messages
2,977
Location
West is best
Still in under investigation means the exact cause may not be known but there is enough data and enough has been done to stabilise the link enough to remove the approach control.
Or to put it another way, permission given for a return to normal working, but the fault is still open (also known as "left on test").

Or more than one actual faulty unit / cable or suspected unit / cable / cause may have been identified. With the most likely or worse having been dealt with. Leaving some other work remaining. Maybe due to having to wait for spares to arrive or for a suitable "wheels free" time slot.

The trouble is, with some intermittent faults, only the passage of time can reveal if the system will be reliable. And sometimes, it's hard to know for certain until normal working is back in operation. Been there, done that. If the desired outcome, everything is fine and stays that way, over 24 hours (or however long), book it back in working order. Or you may get a call five minutes, ten minutes or maybe an hour later "it's done it again!"...
 

Tilting007

Member
Joined
21 Oct 2024
Messages
143
Location
Rugby
Correct




Not correct, as the delays will largely be ‘sub threshold’ and not accounted for financially.

It has, however, completely screwed On Time and Time to 3 punctuality, which has caused much consternation.
Delay was around 3 mins per train with the delay totalling around 14k mins since the incident started late March.
 

Bald Rick

Veteran Member
Joined
28 Sep 2010
Messages
32,372
Delay was around 3 mins per train with the delay totalling around 14k mins since the incident started late March.

Thanks, that sort of demonstrates my point. Well over 300 trains a day use that stretch on the fasts, if they had all racked up 3 minutes attributed delay the incident over the almost 2 months it would have been a 50k mins+ incident.

Clearly a big incident, and one that needed resolving quickly.
 
Last edited:

Top