70000 Britannia is heading the other way with the Shrewsbury Cathedrals Express (1555 Shrewsbury - London Waterloo) and should now pass Winchfield at around 2205 - it's currently in the Andover area, 20 down. If that were to break down too...
And yes, Tangmere is the loco involved in the working which has failed.
I thought Tangmere was hauling this one? Or did it only haul in one direction?
I'd just been looking at the two workings (as a friend of mine saw the outbound at Southampton Central this morning) and it didn't initially strike me that the train has broken down at Winchfield. Looking at NRES, it appears that nothing can currently call there, Fleet or Hook...I guess that would be due to a lack of crossovers between the slows and fasts between the stations
70000 Britannia isShrewsbury..he other way with the Shrewsbury Cathedrals Express (1555 Shrewsbury - London Waterloo) and should now pass Winchfield at around 2205 - it's currently in the Andover area, 20 down. If that were to break down too...
And yes, Tangmere is the loco involved in the working which has failed.
Britannia was over an hour late into shrewsbury.I thought it was diesel from at leaat Bristol to Waterloo poss all the way back following the late loss of Tornado?
Still no idea why it was booked to call at Oakham for nine minutes - I think it surprised a few of the bystanders when it passed through at a fair speed!Not all end up in the mire, The Tyeseley to Ely special yesterday with Earl of Mount Edgcumb ended up 14 mins early though Oakham much to the disappointment of those that turned up on time :roll:
and arrived 1 min early at Ely .
The return was just 1 min late back into Birmingham after being early at various stages due to signal checks on the final leg so it can be done
http://www.realtimetrains.co.uk/train/U54624/2013/11/23/advanced
It has also terminated at Basingstone 200 mins late. Wonder what will happen with passengers needing to get back to Weymouth...
I regret I only have details that a diesel loco may be involved, and it wasn't confirmed to me, so I'm not sure!
Still no idea why it was booked to call at Oakham for nine minutes - I think it surprised a few of the bystanders when it passed through at a fair speed!
Welcome to the forum, and I totallyI despair sometimes about the negative attitude of we Brits. True this loco failed and theres no official reason yet but, its the 21st Century when nobody moves until a Risk Assessment has been performed. So when a train fails away from a Station, rather than comment sarcastically, or ask why it has taken so long to repair it, critics should ask themselves what would have done to make things safe and then get their paying public to the end of the journey with the minimum of fuss while trying to keep costs down; and then, ask how long it would take.
I do worry that some of the comments here are a bit harsh. I am a Railfan, not an anorak nor a trainspotter and Im sad when anything goes so badly wrong that it threatens my future enjoyment and that of others.
We should commend the work done by the Support Crew and Network Rail to safely get the thing moved to a refuge inside four hours, working in the dark and on the road (not at the roadside!). A Well done to them, I think.
Welcome to the forum, and I totally
agree with you.
Locomotive failure near Winchfield, Hampshire
The RAIB is investigating the failure of a steam locomotive hauling a passenger train, which occurred between Fleet and Winchfield stations on Saturday 23 November 2013.
At about 18:50 hrs, train 1Z94, the 17:48 hrs charter service from London Waterloo to Weymouth, was approaching Winchfield, where it was due to stop for the locomotive to take on water. While the train was travelling at about 40 mph, the right-hand connecting rod of the locomotive, former British Railways (Southern Region) 4-6-2 34067 “Tangmere”, became detached at the leading end (referred to as the small end), and dropped down. The end of the detached rod struck the conductor rail, and there was some electrical flashing. This was noticed by the locomotive crew, and the driver stopped the train immediately, about one mile outside Winchfield station. After running along the conductor rail for some distance, the connecting rod dropped onto the sleeper ends just before the locomotive came to rest.
The locomotive’s support crew dismantled the connecting rod, and the train was then assisted by the diesel locomotive that was attached to its rear as far as Basingstoke, where the passengers transferred to another train to continue their journey.
The RAIB’s preliminary examination found that the small end assembly, in which the connecting rod is secured in the crosshead by a gudgeon pin and associated nut and cotter, had come apart. The gudgeon pin was found intact, lodged on the locomotive, but the nut and cotter have not yet been recovered.
The RAIB’s investigation will seek to identify the sequence of events leading to the connecting rod becoming detached. It will include the design, manufacture, installation and maintenance of the components making up the crosshead and piston assembly, and relevant aspects of the operation and maintenance of the locomotive.
The RAIB would be pleased to hear from anyone who has a photograph or video recording showing detail of the right-hand side of Tangmere, taken at Waterloo or subsequently on the journey during the evening of Saturday 23 November.
The RAIB’s investigation is independent of any investigation by the Office of Rail Regulation.
The RAIB will publish its findings, including any recommendations to improve safety, at the conclusion of its investigation. This report will be available on the RAIB website.
what is its status as I note that some booked workings have been cancelled due to "uncertain locomotive avaliability" the two Swanage Belle specials have both been worked by the black 5 44932 and todays comment "wot no diesel" as the down train came through without the 47 on the rear
Maybe we should get these kettle jobs off the mainline, well at least generally off the major routes anyway.
OK I will get my coat
Some people just have no soul. Who could possibly want to see 'Sutherland' or a 'Streak' bumbling along a heritage line at 25mph instead of in its natural environment, speeding along a main line with 12 on?
Mind you, anyone who refers to a steam locomotive as a 'kettle' has already indicated that they not capable of appreciating such sights and sounds. :roll:
You've clearly never seen the issues caused by loads of steam engine enthusiasts crowding round an engine with staff repeatedly shouting at the to keep the platform edges clear so normal services can run safely and the crowd paying no attention.