wensley
Established Member
43185 being the high profile in swallow livery!
And 37254!
43185 being the high profile in swallow livery!
How on earth do you do a "pull-away test" with unmotored stock?
It is, during the Bromsgrove closure the attachment comes off 1M41 1007 ex Paignton which terminates at Bristol Temple Meads. The reason why the Dundee is a 221/220 and not a 220x2 during the closure is because it now formed by the 0828 from Penzance because of the extended journey time associated with going via Kidderminster, this train is booked a 221 (normally through to Glasgow).
Works here, thanks!
Is that a Bardic I spy playing tail-lamp?![]()
Perhaps it was the other half?
They'll have a job recovering it to Phillips Marsh just yet, the power car is missing a coupler at the rear end! The plan at present is to reunite it with the rest of the set eventually though.
I suppose there is a chance that the split may have done some damage to the pipes on the back of the power car so it'll be a bit more complex to get it shifted.
Are there XC facilities in Bristol? If not might GWR lend a helping hand to get it shifted?
I think the problem is that it's facing the wrong way.Perhaps the PC at Bristol Parkway can move under it's own power. There's no problem working a PC on it's own, after all it got there from the point of slipping.
I think the problem is that it's facing the wrong way.
When HST coaches are being coupled, is a pull-away test done at all?
btw, that 08 must be one of the few if not the only item of loco/unit/rolling stock in use in the swallow livery
86213 isn't, its in Bulmarket branded ETL colours.86213 and some mark 1 coaches are also in this livery.
Eeek hope the driver is okay.
The RAIB report for this could make for rather interesting reading.Hi all,
Looking on TyrellCheck, Cross Country have said that their 1S51 12:24 Exeter St Davids to Glasgow Central has divided in the Lawrence Hill area.
1S51 has divided in the Lawrence Hill area.
The front power car will be taken to Bristol Parkway, and the rear power car and passenger coaches to return to Temple Meads.
I hope everyone is ok, I'm guessing it must have been a shock to the passengers and train crew on this train.
The RAIB report for this could make for rather interesting reading.
Dave
Watching the movements on the map gave the impression the train was emptied before movement, 1S51 standing a considerable time outside TM (although this may have been congestion with trains that couldn't go) and a southbound train standing alongside 0S51 at Stapleton Road.
Why wouldn't the driver be OK? It hasn't crashed, blown up, caught fire, etc., it's just come uncoupled.
Being in charge of a high speed piece of machinery while it is undergoing failure is likely to shake up anyone, nevermind a person who knows more than most do about the things a failure can cause.
If I was driving my train and found out half of it was no longer attached then I wouldn't be best pleased.Drama queen....
It wasn't travelling at high speed and the train "failed safe", exactly as it was designed to do.
Drama queen....
It wasn't travelling at high speed and the train "failed safe", exactly as it was designed to do.
If I was driving my train and found out half of it was no longer attached then I wouldn't be best pleased.
Would you give it a stern talking to and tell it to buck up its ideas?
Would you give it a stern talking to and tell it to buck up its ideas?
I would tell it that it has to pull itself together!Would you give it a stern talking to and tell it to buck up its ideas?
Perhaps you need to re-read the post I replied to. "Scratch his head a little" - absolutely. "Shake anyone up" - errrr, no.Perhaps you need to apply some human element to the situation as when the driver felt the cold breeze behind him and looked round to see no train he probably had to scratch his head a little
I would tell it that it has to pull itself together!
How on earth do you do a "pull-away test" with unmotored stock?
It Has been suggested elsewhere that there has been a failure of the Buckeye Pin. HST PC will no doubt have to have some attention to the multi cables - such things don't appreciate being ripped out!
They'll have a job recovering it to Phillips Marsh just yet, the power car is missing a coupler at the rear end! The plan at present is to reunite it with the rest of the set eventually though.
Would you give it a stern talking to and tell it to buck up its ideas?